Just little fun in 100F+ temps today... old oil had 2,900 miles on it.. this was the original oil used with the turbo install plus multiple dynos, datalogs, and a few passes at the track.. LOOKED good.. no metal bits found with a magnet...
Double checked for leaks etc and everything looks good.. the output seal on the PTU is still has a little shine on it but nothing serious yet..
So we now have fresh oil to continue the revisions on my turbos.. Matt is having to remap the tables since my car isn't responding the same way as his or anyone elses.. mine is VERY boost happy..
Progress has been made as the throttle is now opening all the way between shifts in a controlled manner so thats a plus.. keeping my fingers crossed that it will be good to go in the next couple revisions.. then onto the E30 revisions which shouldn't be near as bad since Matt said he can take the new mapping and apply them to the E30 tune..
I will say that getting these turbo's dialed in has been painful, BUT even the auto octane tune is a new beast with it almost done.. can't wait to see how the E30 feels.
Matt could cheat and apply parameters to get the car to respond correctly, but him and I discussed and agreed it would be better to have the turbos dialed in 100% as opposed to short cuts.