polskifacet
New member
Looking at derfdog's log, his frp drops to 9 MPa and recovers but the tune is also running 12.5 afr vs w.e LMS is wanting which looks to be 11.
polskifacet said:Looking at derfdog's log, his frp drops to 9 MPa and recovers but the tune is also running 12.5 afr vs w.e LMS is wanting which looks to be 11.
MiWiAu said:Not sure if it helps or not, but here is a log of my XSport in cold(er) temps. I'm not certain, but I assume the fuel system is the same as the SHO?
I also had the AJP boost regulator installed, so it would have helped minimize pressure drops during shifts.
Ambient: 8.6 F
IAT2: mid 50s at start of runs
Target Boost: 14.5 PSI
Note, since this log was taken, I've changed the regulator boost reference and moved down to 15.95 PSI springs, which helps with the pressure drops. We've not had any bitter cold since making these changes, but if it gets back down close to 0, I will log again for comparison.
AJP turbo said:MiWiAu said:Not sure if it helps or not, but here is a log of my XSport in cold(er) temps. I'm not certain, but I assume the fuel system is the same as the SHO?
I also had the AJP boost regulator installed, so it would have helped minimize pressure drops during shifts.
Ambient: 8.6 F
IAT2: mid 50s at start of runs
Target Boost: 14.5 PSI
Note, since this log was taken, I've changed the regulator boost reference and moved down to 15.95 PSI springs, which helps with the pressure drops. We've not had any bitter cold since making these changes, but if it gets back down close to 0, I will log again for comparison.
This log might not be best either...you show a substantial fuel pressure drop because the throttle is open which allows the boost to spike and the spring in the gate mod was too high but i think at least you see fuel pressure recover at a higher boost level than polski
polskifacet said:Lines are all perfect, no distortion of any sort. I wasn't able to get the pump out, will try to source the tool tomorrow, worst case I have to buy it for $50 online.
polskifacet said:I had to buy the damn tool, apparently no one has it in Chicago lol. Scheduled delivery tonight so hopefully I can capture that log too.
polskifacet said:Changed the pump, it was a SOB even with the tool. Logs look better but I attribute that completely to the fact its 20f warmer today then previous log. Still drops down to 1000 psi with kick down from 5th to 2nd. Logs 6 and 7 are with the new lpfp. Now the ball is in LMS's court since it must be a tune problem which seems to heavily be linked to ambient temp. Lmk what you guys think.
Note: no Hesitation on these runs
http://polskifacet.dynu.com:55698/uploader/uploads/Pictures/Logs/
StealBlueSho said:polskifacet said:Changed the pump, it was a SOB even with the tool. Logs look better but I attribute that completely to the fact its 20f warmer today then previous log. Still drops down to 1000 psi with kick down from 5th to 2nd. Logs 6 and 7 are with the new lpfp. Now the ball is in LMS's court since it must be a tune problem which seems to heavily be linked to ambient temp. Lmk what you guys think.
Note: no Hesitation on these runs
http://polskifacet.dynu.com:55698/uploader/uploads/Pictures/Logs/
Most tunes have an issue with the downshift from 5th to 2nd... not completely unusual..
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AJP turbo said:Even at low temps the commanded boost of his tune is TOO low to be a problem on E10 pump gas as long as the fuel system is ok and the tune or strategy is not goofed up